morgan was running state records on the biggest producing oil well, and as you know those numbers are averaged out over 30 days, the Ip flows were off the dial!!
putting it into perspective.. the AZZ francis dilworth 2h well produced a total of 14612 bo over 90 days, morgan did 38,500 in 30 days.. so twice the 90 day flow rate of the other well in one month..
monster.. absolutely!!
can you see why AWE is putting in a bid for ADI at .40 and not chasing down the far bigger acreages that the AZZ region holds??
kowalik 2 needed to be drilled, i am aware that locals in the ami were very certain that the hilcorp jvp would not want to drop the acres to other competitors, so the jvp imho are wise to keep the leases and are completing kowalik 2h now. with that very nice flow rate on morgan, the wells are paying themselves off in the 90 day region..
kowalik 2H and morgan are going to be side by side in terms of how the sit on the trend..
my view is that without the awe offer,, the adi share would have been trading in the low to mid .30's by now with that morgan announcement.. and heading towards the near term .47 price target that harleys were talking about..
the drilling of kowalik 2 imho and the knowledge that the jvp are deciding to drill leases before expiry rather than let them go, and who wouldnt with the spectacular results thus far, makes it a very busy time in the very near future..
sure awe will be hopeful of a current bid being looked at, but imho the price is not going to be that attractive as the days roll by..
with that shocking response from awe yesterday, it almost was trying to say that adi would never achieve the current price on its own merits.. that will be a very tough one to get over later as i think there is momentum and weight to say adi would be mighty close to these bid prices on their own accord
awe imho is saying you will be worse off without a bid.. well maybe a few cents worse off, but i think there is better upside in adi and personally i would like to see adi trade 6 months more and sell on market then..
Wow, Morgan is a monster producing almost 1,300 BOCD.
Rancho finished, results will be next week I'm guessing.
Kowalik#2, now that brought a smile to my face. What also brought a big grin was the quote,
"The Kowalik redrill will be the first of a number of Sugarloaf wells to be drilled during this calendar year where all Joint Venture partners will contribute to costs and derive revenue on a post farm out basis."
Lots more wells in the AMI by years end, bring it on.
AWE 40c, LMFAO hahahahahahah
Hi rock86
I and others agree with you yet the SP remains static on volumes of just over 1.2m.
I would have thought that the release this morning would have had an immediate impact on the SP especially given that for the first time there are definite plans to drill more wells this year.
Any thoughts?
Hi rock86
I and others agree with you yet the SP remains static on volumes of just over 1.2m.
I would have thought that the release this morning would have had an immediate impact on the SP especially given that for the first time there are definite plans to drill more wells this year.
Any thoughts?
announcement out...
Rancho Grande Initial Production Rate
The Rancho Grande #1H well commenced flow back on 1st June 2010 and has been flowing on a reduced choke setting. The maximum production rate over a consecutive 24 hour period has been:-
Rancho Grande #1H
Gas Production Rate 3.19 (mmscf/d)
Condensate Production Rate 1170 (bbls/d)
Average Daily Equivalent Gas Rate 18.00 (mmscfe/d)*
* The equivalent gas rates have been calculated to reflect value using a 12:1 conversion ratio for condensate and a 25% uplift on gas equivalent volumes due to the high calorific value of the produced gas.
The intent of producing the well on a reduced choke setting is to investigate whether a limited reservoir drawdown can improve decline rates and the ultimate recovery from the wells. It should be understood that the well is capable of flowing at a higher rate, but this investigation is part of the ongoing efforts to optimise the commerciality of the field. In addition, the following comments should be considered:-
• This is an initial production rate that has been observed during clean up and as such is not yet indicative of a short or long term production profile.
• The well still has considerable fluid to recover from the fracture stimulation.
• The well is currently producing through the production casing. A production tubing string
will be installed in due course.
367 bbls per 1mm cfg looks pretty good. Kowalik 1 started delivering at about that rate. Looking good for Kowalik 2.
hey agent, when do you think they will have the reserve upgrade figures out??
Before the end of the month?
"i think GS would rather just get a nice chunk that AWE have to pay them handsomely for...."
They'd have to pay us the same or more......https://www.aussiestockforums.com/forums/images/smilies/smile.gif
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